First off merry christmas everyone! Hope you are all full of xmas day leftovers today.
After xmas dinner today (I had it with the in-laws yesterday) I decided to start the engine rebuild. All that has been done today was oil leak detection, coolant leak detection and a compression test.
I've had an annoying oil leak since I have had the car and it seemed to be coming from behind the cambelt covers (that's why i pulled them off and changed all oil pump area seals and gaskets a while back), however it didn't stop the leak so today i have removed the covers looking for the leak yet again. It was bone dry inside and I have found that it is coming from the back of the rocker cover gasket which is a pain as I changed this following correct procedure. The oil was travelling down the wiring harness and spreading around the back of the engine.
The Lude has also developed a water leak coming off of the body of the water pump. Under a test pressure of 1.1bar it is slowly dripping from the bleed hole, showing the the inside of the water pump is f***ed. I need to call up parts tomorrow as this should still be under guarantee.
Before removing the engine I wanted to do a compression test to check general health and I am please to say that I got some healthy numbers back:
cylinder 1: 240 psi
cylinder 2: 240 psi
cylinder 3: 250 psi
cylinder 4: 235 psi
The only problem is the sevice manual states that they should be around 185 psi. High numbers could possibly be carbon build-up in the combustion chamber but the numbers seem a bit too high for that. I'm guessing the workshop compression testing equipment is faulty.
My H-tune goodies arrived finally! It took a while due to lack of stock on some washer jets that I ended up cancelling, but apart from that I can't fault their service and would buy from H-tune again. The Blox gear knob is very heavy, it's hard to comprehend how something that small can be so heavy!
